follow ft86club on our blog, twitter or facebook.
FT86CLUB
Ft86Club
Delicious Tuning
Register Garage Community Calendar Today's Posts Search

Go Back   Toyota GR86, 86, FR-S and Subaru BRZ Forum & Owners Community - FT86CLUB > Technical Topics > Software Tuning

Software Tuning Discuss all software tuning topics.


User Tag List

Reply
 
Thread Tools Search this Thread
Old 04-27-2022, 12:39 PM   #1
blsfrs
Senior Member
 
blsfrs's Avatar
 
Join Date: Dec 2018
Drives: 2013 frs base
Location: central Virginia
Posts: 1,115
Thanks: 1,729
Thanked 914 Times in 474 Posts
Mentioned: 12 Post(s)
Tagged: 0 Thread(s)
High rpm bogging

Long history in a short period. NA engine rebuilt after rocker arm/timing chain issue. What would cause the ignition timing advance to drop at wot? Still waiting for my tuner to get back to me.



https://datazap.me/u/blsfrs/log-1644...&data=10-20-21
blsfrs is offline   Reply With Quote
Old 04-30-2022, 10:47 AM   #2
blsfrs
Senior Member
 
blsfrs's Avatar
 
Join Date: Dec 2018
Drives: 2013 frs base
Location: central Virginia
Posts: 1,115
Thanks: 1,729
Thanked 914 Times in 474 Posts
Mentioned: 12 Post(s)
Tagged: 0 Thread(s)
Funnier behavior. If I push the pedal 3/4 (under load, 2nd and 3rd gear pulls) to the floor, the rpms go from 3000 to 7300, no problem.



If I push the pedal 4/4, at around 5000, the engine bogs like hitting a rev limiter and my ignition advance drops to 3*-5*. The point that the advance drops can vary from 4500 to 7000.


Are there any diagnostics I can do while waiting to hear back from my tuner, Said he's going to look at my logs this weekend.
blsfrs is offline   Reply With Quote
Old 05-02-2022, 09:32 AM   #3
NoHaveMSG
Senior Member
 
NoHaveMSG's Avatar
 
Join Date: Jan 2018
Drives: Crapcan
Location: Oregon
Posts: 11,163
Thanks: 18,156
Thanked 16,323 Times in 7,381 Posts
Mentioned: 107 Post(s)
Tagged: 0 Thread(s)
Garage
Did something get changed in the tune recently or is this just since the rebuild?
__________________
"Experience is the hardest kind of teacher. It gives you the test first and the lesson afterward." -Oscar Wilde.
NoHaveMSG is offline   Reply With Quote
The Following User Says Thank You to NoHaveMSG For This Useful Post:
blsfrs (05-02-2022)
Old 05-02-2022, 11:22 AM   #4
shr133
Senior Member
 
shr133's Avatar
 
Join Date: Nov 2015
Drives: 2013 FRS
Location: WISCONSIN
Posts: 101
Thanks: 39
Thanked 25 Times in 21 Posts
Mentioned: 14 Post(s)
Tagged: 0 Thread(s)
Garage
Quote:
Originally Posted by blsfrs View Post
Long history in a short period. NA engine rebuilt after rocker arm/timing chain issue. What would cause the ignition timing advance to drop at wot? Still waiting for my tuner to get back to me.



https://datazap.me/u/blsfrs/log-1644...&data=10-20-21
is it running lean??? or rich??? when you go to full throttle it uses a different part of the map, but something physical or in the tune is off.... not getting enough fuel???
__________________
Enkei TS9 18 X 8, Michelin Sport 4S 225 40 18, Flex Fuel, Edelbrock Supercharger, P & L header, Nameless front pipe, V1 cat back, Aluminum Driveshaft, pvc delete, med duck bill, KW V3, Whiteline 20 and 18 mm bars, Buddy Club and SPL control arms, Toe Arms, motor and trans mounts, Whiteline bushings, SHR stage II tune.
shr133 is offline   Reply With Quote
The Following User Says Thank You to shr133 For This Useful Post:
blsfrs (05-02-2022)
Old 05-02-2022, 12:32 PM   #5
blsfrs
Senior Member
 
blsfrs's Avatar
 
Join Date: Dec 2018
Drives: 2013 frs base
Location: central Virginia
Posts: 1,115
Thanks: 1,729
Thanked 914 Times in 474 Posts
Mentioned: 12 Post(s)
Tagged: 0 Thread(s)
Quote:
Originally Posted by NoHaveMSG View Post
Did something get changed in the tune recently or is this just since the rebuild?
Here's the timeline (and I didn't even mention the broken driveshaft).


March 2021: Ingested something in #3. Ejected intake rocker arms, broke timing chain. Complete rebuild by Cody Dawson. Injectors serviced by Injector Pulse. Engine reinstalled September 2021



PROBLEMS SINCE REINSTALL


Intermittent P0219a and P0119f (AFR codes) and decreased power.



Replaced: MAF, MAP, upstream 02 sensor. No change.


January 2022: PTuning: No problems found. Retuned. NEW PROBLEM: Upon picking car up, found bogging at 5500-6500rpm. On the way to Charlottesville the CEL for secondary 02 came on but hasn't come on again. No improvement with replacement of throttle body.


February-March 2022; Bogging/decreased power worsened to the point where the car wouldn't go over 35-40 mph. Upstream cat removed after temp/back pressure tests. Immediate improvement in power up to 6000rpm then bogs like hitting rev limiter. Sometimes improves with 3-4 3rd gear pulls but bogging returns next drive cycle. Installed Nameless 2.5" catted midpipe: No change in bogging. CEL for P0219a and P0119f came on last week.


A couple of weeks ago went back to PTing. Their guy could not reproduce bogging. He then rode with me and I reproduced it with him in the car. He and their tuner went out to data log but could not reproduce bogging. I finally was able to send them an Ecutek datalog and am waiting to hear back from them.
blsfrs is offline   Reply With Quote
The Following User Says Thank You to blsfrs For This Useful Post:
NoHaveMSG (05-02-2022)
Old 05-02-2022, 12:40 PM   #6
blsfrs
Senior Member
 
blsfrs's Avatar
 
Join Date: Dec 2018
Drives: 2013 frs base
Location: central Virginia
Posts: 1,115
Thanks: 1,729
Thanked 914 Times in 474 Posts
Mentioned: 12 Post(s)
Tagged: 0 Thread(s)
Quote:
Originally Posted by shr133 View Post
is it running lean??? or rich??? when you go to full throttle it uses a different part of the map, but something physical or in the tune is off.... not getting enough fuel???
Tuner at Ptuning says everything looks good.
blsfrs is offline   Reply With Quote
Old 05-02-2022, 01:08 PM   #7
NoHaveMSG
Senior Member
 
NoHaveMSG's Avatar
 
Join Date: Jan 2018
Drives: Crapcan
Location: Oregon
Posts: 11,163
Thanks: 18,156
Thanked 16,323 Times in 7,381 Posts
Mentioned: 107 Post(s)
Tagged: 0 Thread(s)
Garage
Quote:
Originally Posted by blsfrs View Post
Here's the timeline (and I didn't even mention the broken driveshaft).
Can you log what the sensor voltage outputs are in Ecutek? I wonder if you have something going out or range on the higher end. Also hard to tell if it is picking up any knock and that is why it is pulling timing, though I doubt this is the case. I'd imagine the PT gus have looked at that already. It's hard to tell what's the chicken/egg.
__________________
"Experience is the hardest kind of teacher. It gives you the test first and the lesson afterward." -Oscar Wilde.
NoHaveMSG is offline   Reply With Quote
The Following User Says Thank You to NoHaveMSG For This Useful Post:
blsfrs (05-02-2022)
Old 05-02-2022, 06:22 PM   #8
blsfrs
Senior Member
 
blsfrs's Avatar
 
Join Date: Dec 2018
Drives: 2013 frs base
Location: central Virginia
Posts: 1,115
Thanks: 1,729
Thanked 914 Times in 474 Posts
Mentioned: 12 Post(s)
Tagged: 0 Thread(s)
Quote:
Originally Posted by NoHaveMSG View Post
Can you log what the sensor voltage outputs are in Ecutek? I wonder if you have something going out or range on the higher end. Also hard to tell if it is picking up any knock and that is why it is pulling timing, though I doubt this is the case. I'd imagine the PT gus have looked at that already. It's hard to tell what's the chicken/egg.
Here is the Ecutek log. I mostly don't know what I'm looking for but I can see the ig timing drop. Any Ideas? Thanks



https://datazap.me/u/blsfrs/log-1651...og=0&data=7-12
blsfrs is offline   Reply With Quote
Old 05-02-2022, 07:33 PM   #9
NoHaveMSG
Senior Member
 
NoHaveMSG's Avatar
 
Join Date: Jan 2018
Drives: Crapcan
Location: Oregon
Posts: 11,163
Thanks: 18,156
Thanked 16,323 Times in 7,381 Posts
Mentioned: 107 Post(s)
Tagged: 0 Thread(s)
Garage
Quote:
Originally Posted by blsfrs View Post
Here is the Ecutek log. I mostly don't know what I'm looking for but I can see the ig timing drop. Any Ideas? Thanks



https://datazap.me/u/blsfrs/log-1651...og=0&data=7-12
That is strange. I was hoping to see a hardware issue pop out but maf is stable as is afr so I doubt the O2 is acting up. KC is 0 with a tiny bit of KC learned. We are over my head. Maybe Tomm or Steve will chime in. I wonder if something else is causing the timing compensation table to wig out and drop out the advance. Any missfires? It for sure can't rev out with it pulling timing that far out.
__________________
"Experience is the hardest kind of teacher. It gives you the test first and the lesson afterward." -Oscar Wilde.
NoHaveMSG is offline   Reply With Quote
Old 05-02-2022, 08:03 PM   #10
blsfrs
Senior Member
 
blsfrs's Avatar
 
Join Date: Dec 2018
Drives: 2013 frs base
Location: central Virginia
Posts: 1,115
Thanks: 1,729
Thanked 914 Times in 474 Posts
Mentioned: 12 Post(s)
Tagged: 0 Thread(s)
Quote:
Originally Posted by NoHaveMSG View Post
That is strange. I was hoping to see a hardware issue pop out but maf is stable as is afr so I doubt the O2 is acting up. KC is 0 with a tiny bit of KC learned. We are over my head. Maybe Tomm or Steve will chime in. I wonder if something else is causing the timing compensation table to wig out and drop out the advance. Any missfires? It for sure can't rev out with it pulling timing that far out.
Lately this car has cornered the market on strange. I get no indication of missfires. As I said earlier, if I hold the pedal at 3/4, it will rev to 7300rpm. If I really floor it , it bogs.


I noticed that none of the PTuning drivers seemed to change my seat position. I have long legs. So, I question if those drivers could push the gas pedal as far as I can. Also, the car was tuned with a failing cat.
blsfrs is offline   Reply With Quote
Old 05-02-2022, 11:25 PM   #11
makinen
Senior Member
 
makinen's Avatar
 
Join Date: Jan 2013
Drives: Toyota 86
Location: South Korea
Posts: 267
Thanks: 127
Thanked 201 Times in 115 Posts
Mentioned: 5 Post(s)
Tagged: 0 Thread(s)
Quote:
Originally Posted by blsfrs View Post
Here is the Ecutek log. I mostly don't know what I'm looking for but I can see the ig timing drop. Any Ideas? Thanks



https://datazap.me/u/blsfrs/log-1651...og=0&data=7-12
AFR looks too rich at high RPM. Way beyond needed. Out of the range that the stock O2 sensor can handle.
__________________
/* Custom underbody panels and diffuser
Custom electric water pump and PWM controller
HKS GT EL header, 17MY intake manifold */
makinen is offline   Reply With Quote
The Following User Says Thank You to makinen For This Useful Post:
blsfrs (05-03-2022)
Old 05-03-2022, 02:49 AM   #12
Ultramaroon
義理チョコ
 
Ultramaroon's Avatar
 
Join Date: Sep 2014
Drives: a 13 e8h frs
Location: vantucky, wa
Posts: 31,869
Thanks: 52,132
Thanked 36,520 Times in 18,921 Posts
Mentioned: 1107 Post(s)
Tagged: 9 Thread(s)
What is going on with the DI from 4.5 to 5.5 seconds into that log? Fuel rail pressure too. Like an intermittent electrical something cutting out from vibration. Red herring? it doesn't happen in the second pull. I'm always afraid to join in on these discussions.
__________________
Ultramaroon is offline   Reply With Quote
The Following User Says Thank You to Ultramaroon For This Useful Post:
blsfrs (05-03-2022)
Old 05-03-2022, 06:23 AM   #13
tomm.brz
Senior Member
 
Join Date: Jan 2017
Drives: brz 2017 hksv2
Location: italy
Posts: 2,196
Thanks: 500
Thanked 1,067 Times in 775 Posts
Mentioned: 65 Post(s)
Tagged: 0 Thread(s)
Something is quite off mechanically/electronically, also we can t see the tune or if he used custom maps too so really can t help, just look to me that something is too off to be tune related
tomm.brz is offline   Reply With Quote
The Following User Says Thank You to tomm.brz For This Useful Post:
blsfrs (05-03-2022)
Old 05-03-2022, 08:56 AM   #14
blsfrs
Senior Member
 
blsfrs's Avatar
 
Join Date: Dec 2018
Drives: 2013 frs base
Location: central Virginia
Posts: 1,115
Thanks: 1,729
Thanked 914 Times in 474 Posts
Mentioned: 12 Post(s)
Tagged: 0 Thread(s)
Quote:
Originally Posted by makinen View Post
AFR looks too rich at high RPM. Way beyond needed. Out of the range that the stock O2 sensor can handle.
Good observation. I didn't see that before. It looks like the afr goes rich when the timing advance drops. Maybe it unburnt fuel as a result of lack late spark?
blsfrs is offline   Reply With Quote
 
Reply


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump

Similar Threads
Thread Thread Starter Forum Replies Last Post
car bogging when coming to stop Qball1754 Engine, Exhaust, Transmission 10 06-06-2019 11:39 AM
Engine bogging down FRiSson Issues | Warranty | Recalls / TSB 6 08-14-2015 08:07 PM
Vortech FR-S Bogging RPM AND STALL ScionFR-S Forced Induction 9 07-24-2015 05:52 PM
random bogging/stalling - no cel though edsbreezy Issues | Warranty | Recalls / TSB 5 04-22-2014 09:58 PM
Transmission Dry Sound & Bogging jjkerr626 Engine, Exhaust, Transmission 3 06-11-2013 12:10 AM


All times are GMT -4. The time now is 01:30 AM.


Powered by vBulletin® Version 3.8.11
Copyright ©2000 - 2024, vBulletin Solutions Inc.
User Alert System provided by Advanced User Tagging v3.3.0 (Lite) - vBulletin Mods & Addons Copyright © 2024 DragonByte Technologies Ltd.

Garage vBulletin Plugins by Drive Thru Online, Inc.