09-10-2018, 06:22 PM | #631 |
Senior Member
Join Date: Mar 2017
Drives: Q5 + BRZ + M796
Location: Santa Rosa, CA
Posts: 7,884
Thanks: 5,668
Thanked 5,806 Times in 3,300 Posts
Mentioned: 70 Post(s)
Tagged: 0 Thread(s)
|
__________________
My Build | K24 Turbo Swap | *K24T BRZ SOLD*
|
09-10-2018, 06:45 PM | #632 |
Senior Member
Join Date: Jun 2013
Drives: GBS BRZ Harrop SC/PTuning Header
Location: NM, USA
Posts: 152
Thanks: 82
Thanked 93 Times in 49 Posts
Mentioned: 6 Post(s)
Tagged: 0 Thread(s)
|
Ran into a problem with my Harrop SC '13. Whenever I am stopping with the clutch in and in neutral, the engine dies. Recently rerouted some vacuum lines back to stock configuration on the car and had to take off the airbox (with maf) and disconnect the wiring loom extension that reaches to the maf, throttle body, IAT, and MAP.
Any suggestions? Is it as easy as cleaning the MAF or is this a larger issue like a vacuum leak from a hose that I missed? The engine power is fine, but runs rich. If I can keep the throttle in using toe-heel, i can keep the engine running by keeping the rpm above 1.4k. |
09-10-2018, 08:35 PM | #633 | |
TRACKBREAD
Join Date: Mar 2016
Drives: 2013 BRZ
Location: Florida
Posts: 3,929
Thanks: 2,660
Thanked 4,029 Times in 1,896 Posts
Mentioned: 30 Post(s)
Tagged: 0 Thread(s)
|
Quote:
Did you plug the bypass valve vacuum line back in? |
|
09-10-2018, 09:50 PM | #634 | |
Senior Member
Join Date: Nov 2016
Drives: 2017 BRZ
Location: USA
Posts: 655
Thanks: 326
Thanked 258 Times in 177 Posts
Mentioned: 3 Post(s)
Tagged: 0 Thread(s)
|
Quote:
Beyond tires, a good damper and stiffer bushings might help. |
|
The Following User Says Thank You to gtengr For This Useful Post: | Irace86.2.0 (09-10-2018) |
09-10-2018, 10:41 PM | #635 |
TRACKBREAD
Join Date: Mar 2016
Drives: 2013 BRZ
Location: Florida
Posts: 3,929
Thanks: 2,660
Thanked 4,029 Times in 1,896 Posts
Mentioned: 30 Post(s)
Tagged: 0 Thread(s)
|
|
09-11-2018, 01:08 AM | #636 |
Senior Member
Join Date: Aug 2014
Drives: '14 981CS, '99 NB1
Location: Oregon
Posts: 1,274
Thanks: 1,234
Thanked 1,201 Times in 631 Posts
Mentioned: 114 Post(s)
Tagged: 2 Thread(s)
|
You're absolutely right. My reference to too soft vs too hard was in relation to the fact that I previously had a my15 FR-S, and that suspension was perfection to me. I always felt the '17 lost some precision in comparison.
|
09-11-2018, 03:40 AM | #637 | |
TRACKBREAD
Join Date: Mar 2016
Drives: 2013 BRZ
Location: Florida
Posts: 3,929
Thanks: 2,660
Thanked 4,029 Times in 1,896 Posts
Mentioned: 30 Post(s)
Tagged: 0 Thread(s)
|
Quote:
Interesting! I went from the original springs on my 13 BRZ to a set of 2017 springs and the car feels more planted! Different driving styles I guess! |
|
09-11-2018, 06:28 AM | #638 |
Senior Member
Join Date: Jun 2013
Drives: GBS BRZ Harrop SC/PTuning Header
Location: NM, USA
Posts: 152
Thanks: 82
Thanked 93 Times in 49 Posts
Mentioned: 6 Post(s)
Tagged: 0 Thread(s)
|
I dont think I ever unplugged it but I'll check when I pull the alternator out this afternoon. Before putting in the AC compresser all vacuum lines on that side were plugged in correctly. There's power under acceleration now. I receive no cell codes after the car stalls/dies. |
09-11-2018, 11:17 AM | #639 |
Senior Member
Join Date: Aug 2014
Drives: '14 981CS, '99 NB1
Location: Oregon
Posts: 1,274
Thanks: 1,234
Thanked 1,201 Times in 631 Posts
Mentioned: 114 Post(s)
Tagged: 2 Thread(s)
|
Well, Toyota/Subaru spec'd different springs/dampers across 13/15/17. So that's not an a/b comparison. Also if you put the 17 springs on 13 dampers, that's a mismatch that would give a completely different experience as well.
|
09-11-2018, 07:14 PM | #641 |
Senior Member
Join Date: Jun 2013
Drives: GBS BRZ Harrop SC/PTuning Header
Location: NM, USA
Posts: 152
Thanks: 82
Thanked 93 Times in 49 Posts
Mentioned: 6 Post(s)
Tagged: 0 Thread(s)
|
Update: Messed with my brake booster line layout which I've suspected of having a crack and noticed while the power was on, the throttle body was humming/buzzing. Unclipped it and all other sensors, checked the connectors then reattached them. After quickly clearing the codes, the vehicle started up and idled for a few minutes while I was logging. Made it a good portion of the way home to a gas station where I refilled (e70) and then all of my problems started over again with the clutch-in stalling.
After a little ways down the road, I noticed if I eased into a stop and was gentle on the clutch disengagement, then the problem went away. Kept logging the entire time. What the heck? |
09-11-2018, 08:08 PM | #642 | |
Senior Member
Join Date: Mar 2017
Drives: Q5 + BRZ + M796
Location: Santa Rosa, CA
Posts: 7,884
Thanks: 5,668
Thanked 5,806 Times in 3,300 Posts
Mentioned: 70 Post(s)
Tagged: 0 Thread(s)
|
Quote:
__________________
My Build | K24 Turbo Swap | *K24T BRZ SOLD*
|
|
09-12-2018, 03:34 PM | #643 | |
Senior Member
Join Date: Aug 2014
Drives: '14 981CS, '99 NB1
Location: Oregon
Posts: 1,274
Thanks: 1,234
Thanked 1,201 Times in 631 Posts
Mentioned: 114 Post(s)
Tagged: 2 Thread(s)
|
Quote:
|
|
The Following User Says Thank You to johan For This Useful Post: | Trefoil (09-15-2018) |
09-15-2018, 03:16 AM | #644 |
Senior Member
Join Date: Jun 2013
Drives: GBS BRZ Harrop SC/PTuning Header
Location: NM, USA
Posts: 152
Thanks: 82
Thanked 93 Times in 49 Posts
Mentioned: 6 Post(s)
Tagged: 0 Thread(s)
|
New update:
The old vacuum lines were fine even after two years of hot weather driving conditions. Rerouting the front vent hose into the correct position has helped with cells. A new ACT HDSS went in and the the old FX400 had totally lost all puck material and was down to just the steel backing! I really recommend shopping with CSG as they both have an amazing price on it while supporting the forums, or to support your local shop. As I'm getting older, working from a garage alone has lost its appeal, since I cant bench press like i used to with a transmission on my chest and it's darn near impossible to work without a lot of investment into more tools. I asked a local subaru mechanic to do the work. After a rather quick install (~2.5 hrs) on his lift, the mechanic noticed an exhaust leak by the header or front overpipe... Which he mentioned could cause the sudden stalling issues at stop lights. Does that make sense? |
The Following User Says Thank You to Trefoil For This Useful Post: | Irace86.2.0 (09-15-2018) |
|
|
Thread Tools | Search this Thread |
|
|
Similar Threads | ||||
Thread | Thread Starter | Forum | Replies | Last Post |
HKS Supercharger owners thread | wbradley | Forced Induction | 1049 | 07-04-2024 04:44 PM |
JDL turbo kit owners thread | yomny | Forced Induction | 1346 | 08-29-2023 11:07 PM |
P&L Turbo kit Owners thread | Hawaiian | Forced Induction | 73 | 07-07-2018 02:31 AM |
Harrop car lip kit? | djdnz | Cosmetic Modification (Interior/Exterior/Lighting) | 15 | 12-15-2015 02:50 PM |
**Offical 213/323/626/818 owners thread** | mr. slim | Southern California | 71 | 10-07-2013 12:58 PM |