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Oh-Oh's, I Think I Broke It!
Hopefully some of the electronics and mechanic gurus might have a better idea of what is going on but ill post a couple of bullet points on what is going on with my car.
Feb 1-3 2013 - FEB 1-3 i got a CEL and the car went into limp mode on the second track day. The codes i got were: P219A Bank 1 Air/Fuel Ratio Inbalance, P000A Intake (a) Camshaft Position Sensor Slow Response Bank 1, P0011 Intake (a) Camshaft Position Timing - Over Advanced (Bank1) I cleared the codes to see if they would pop up again and they did not, i continued for another day and no problems what so ever the car ran fine. Feb 23 2013 1st Session -Yesterday after 5 laps i lost power on the straight for a second or two and my check engine light flashed twice but went away, i kept driving and it did not do it again. 2nd Session -Next session as i turned the car on it puffed a huge cloud of white smoke but it went away and stopped smoking, as i pulled out of the grid it puffed a cloud of smoke again according to a friend. As i came back my belt started whining but then went away after a couple of seconds. 3rd Session -No smoke this time but i lost power on the same straight as session #1 but this time my car lost almost all power and sounded like it was misfiring and sounded like a boxer engine. I pulled up with my dash looking like a christmas tree and the car struggled to idle, i immediately turned her off and checked the codes i got P0011 Intake (a) Camshaft Position Timing - Over Advanced, and cylinder 2 misfire. I thought it might be an electronic glitch like at Cota but i cleared the codes and the car would not turn on. Anybody have a clue what could be wrong? Quick video: [ame="http://www.youtube.com/watch?v=FKwaMESOfPA"]Fr-s misfire - YouTube[/ame] Codes i got FEB 1-3 http://i23.photobucket.com/albums/b3...ps705a8117.jpg http://i23.photobucket.com/albums/b3...ps5a2ab439.jpg http://i23.photobucket.com/albums/b3...ps92eaa3e0.jpg |
Damn dude that doesn't sound good. When did it start doing that?
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Sounds like a shitty tune. Flash it back to stock.
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Gonna be super honest here man...Engines seems done, and it was due to AP pulley... J/K
I agree with above post, seems like a shitty tune. |
Sorry about that. Hope you get that thing up and running soon. I've been enjoying your track day posts.
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Untested tune on a car that hasn't been around long?
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Sounds like my jeep liberty. When it had a stuck lifter and the rocker arms fell off.
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At this stage there is zero chance of blaming on bad OEM ECU. It went to zero right after you flashed it. Gotta pay for play. |
do a leakdown.... check the plugs first!
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I hope this ends up being an "easy" fix...:(
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Dang, hope its nothing serious. I play to track my car as much as you have yours :eek3:
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I hate to say it, but I think your pulley may have done some damage. Be sure to swap it back out if your going to try for warranty.
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It started since feb 1-3 2013 but i have a tune since november 2012 and have ran the car various times since then and didnt have any problems. Quote:
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Here she is sitting all sad on that cold trailer :( http://i23.photobucket.com/albums/b3...ps8ad793a7.jpg |
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