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Old 07-24-2014, 12:24 AM   #29
ThisGuy919
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Originally Posted by kingkai23 View Post
I installed turbo kit..the injectors the fuel pump the ebc ,3 bar map and vaccum lines and clutch were installed by shop prior to tune it just seems weird to me first dyno session and 11 days of street driving the wg port plugs dont come out but on 2nd dyno attempt they all of a sudden came out on the dyno..i wasnt there during the tuning session how would i kno if they werent screwd loose to cover their asses?
Keep in mind of the possibility that they could be loose from the start and they eventually popped off due to more stress from the dyno??? To many variables to put the blame on anyone in particular unfortunately. They could've helped as far as maybe giving you some sort of promise to pay thing instead of asking for payment right away given the situation? (Just what I would've done at least) Sorry to hear this happened though.
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Old 07-24-2014, 12:51 AM   #30
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hope you get it worked out soon man.
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Old 07-24-2014, 01:10 AM   #31
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Sorry about the car man.
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Old 07-24-2014, 01:55 AM   #32
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Im really surpised, i had a shop incorrectly install WG lines on cousins brz, the car overboosted on an FA20crap base map(OVER15PSI) a couple of times and the motor didn't blow :/. The car has since been tuned nemours times and now runs over 12psi on 91 perfectly fine
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Old 07-24-2014, 02:33 AM   #33
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I would ask for logs for all the runs they did that day.

If you have proof that the boost was being controlled in the earlier runs, and then not controlled in later runs (all while under their care), then it is definitely their fault.
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Old 07-24-2014, 03:20 AM   #34
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If they didn't do every single bit of the install, you're on your own. Putting the car on the street and the keys in the mailbox is pretty standard for picking up a car after hours. Should they have waited for you and given you a hug? The dyno is a pretty intense place. Things can and do go wrong there. In the end, you pay to play.

View this as a chance to get a built engine. I'd call up Full Blown, MAP, or Element.
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Old 07-24-2014, 07:40 AM   #35
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nek minnit
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Old 07-24-2014, 11:00 AM   #36
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The wastegate plug coming out is a possibility, but a good tuner and shop should be monitoring boost and that should not have blown your motor. I would ask for more details or proof of what occured when the motor blew. They should have been datalogging the car with EcuTek at the time the motor blew. I would like to hear the other side of the story from @PrimeMotoring and @JuniorAWD.
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Old 07-24-2014, 11:05 AM   #37
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Quote:
Originally Posted by kingkai23 View Post
First dyno session dyno had issues wouldnt display hp/tq graphs but left with 10/11psi 93 map and e85 15/16 psi map..drove it away had to come back to get tuned touched up and the shop had to get the mustang dyno fixed a week later..i dropped off car sun nite..i get a call in am saying they working on fueling issues should be done later get a call later in pm hey your motor blew come get it sorry we blew your car up..you still gotta pay for the tune and the ecutek lic tho which i already paid for at first dyno session...and ofcouse it was the installers fault which was me becuse wg port plugs came out but from the 7th first day of tune thru when i dropped it off back to them on sunday the 19th car ran perfectly fine with just a lil hiccups and hot start issues..basically prime motoring told me to go fuck myself left my car on street and my keys in their mailbox
Well isnt this the furthest from the truth. Kai, i called you and told you exactly what happened but you proceeded to try to blame us. Who installed the kit? We even found another tial wastegate box to show you in the instructions you need to install the caps with loctite which in the picture below shows you did not. Your car was tuned last week and it came back to fix a hot start issue and touch it up. Unfortunately the plugs rattled loose by then and you are trying to pin anything on us. If we installed the kit and this happened, then we would owe you a motor.


You have been in contact with Junior and myself the entire time and no point did we tell you to "fuck yourself." You basically said that to us when you said to leave your car on the street and youll pick it up tonight. None of that gets mentioned though, its just "Prime Motoring blew up my car". Whoever installed the wastegate and did not follow instructions should take responsibility for the car overboosting.

Last edited by PrimeMotoring; 07-24-2014 at 12:17 PM.
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Old 07-24-2014, 11:19 AM   #38
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Quote:
Originally Posted by King Tut View Post
The wastegate plug coming out is a possibility, but a good tuner and shop should be monitoring boost and that should not have blown your motor. I would ask for more details or proof of what occured when the motor blew. They should have been datalogging the car with EcuTek at the time the motor blew. I would like to hear the other side of the story from @PrimeMotoring and @JuniorAWD.
In terms of data logging im sure @JuniorAWD will chime in with that since he has those. I can supply the pictures though.

This is what we find when trying to figure out why the car overboosted.



Tial recommends all fittings be loctited on, even the water fittings. This is a wastegate we had laying around. I didnt have the bag with the airport fittings because it was thrown out after the fittings were loctited and installed to dry.



Noticed the other port was hand tightened on and pulled it off to see if there was loctite applied....none



The other plug is underneath the dyno or somewhere in Kai's car. We could not find it to see but that is what we found. Everyone can play the situation as they please but we can not control hardware issues caused by user error. Like i mentioned, if this was our install, we would be buying Kai a new motor.
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Old 07-24-2014, 11:24 AM   #39
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Old 07-24-2014, 11:50 AM   #40
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Wonder if they have data of what boost blew it up.
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Old 07-24-2014, 12:08 PM   #41
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So why are we fi these cars instead of buying a wrx, sti, genesis 2.0t, 370z, 335i, Ore any turbo car stock, worth factory warranty? So glad I'm gonna stay NA
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Old 07-24-2014, 12:21 PM   #42
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Because its just the game of modding cars. And trust me, I have seen countless WRX's, STI's, Genesis 2.0's and 370s destroy engines all the time, (even stock ones) I don't see how they are any different. And there are plenty of N/A stock FRS/BRZ's that have blown engines as well. There are also plenty of boosted FRS/BRZ's running well without any issues, including my daily driven one.

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So why are we fi these cars instead of buying a wrx, sti, genesis 2.0t, 370z, 335i, Ore any turbo car stock, worth factory warranty? So glad I'm gonna stay NA
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